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HomeMy WebLinkAboutDRC-2012-002054 - 0901a06880314227State of Utah GARY R HERBERT Governor GREG BELL Lieutenant Governor DRC-2012-002054 Department of Environmental Quality Amanda Smith Executive Director DIVISION OF RADIATION CONTROL Rusty Lundberg Director MEMORANDUM TO File THROUGH Phil Goble, Section Manager FROM Russell J Topham, P E DATE September 25, 2012 SUBJECT Cell 1 Liner Repairs Radioactive Matenals License UTl 900479 (RML) and Groundwater Discharge Permit (GWDP) UG370004, Energy Fuels Resources, Lie (EFR) White Mesa Mill, Blanding, Utah EFR has completed repairs to the Cell 1 Imer system As required, EFR provided a detailed report of the repair activity in its 2"^* Quarter DMT Performance Standards Momtonng Report EFR included a root cause analysis with the repair report The repair effort appears to have addressed the findings of the root cause analysis The report appears comprehensive and pertment Repair activities appear appropriate, and field vacuum testmg appears to support a conclusion of successful repair installation On September 20, 2012,1 reviewed field conditions, records and photos of the repair at the mill offices I also interviewed David Turk and Gamn Palmer about the effort Following the repair, crews placed one foot of soil over the liner matenal, thus, I took no photos dunng the inspection ^ Fluid levels in the cell have not returned to an elevation above the repau", and likely will not reach a suitable elevation to test the repair for several weeks Thus, we must rely on the vacuum testing narrative in the report for now I recommend holding this project open until fluid levels approach design maximums in the cell Soon thereafter, readings in the leak detection system can provide positive verification of the efficacy of the repairs One month fi-om the time solution levels reach the design maximum elevation should prove adequate I recommend approving the repair report as sufficient to meet the requirements as presented m Revision I of the Liner Maintenance Provisions, dated October 18, 2009, and with Part IF 2 of the RML History On June 2, 2010, EFR detected fluid in the Cell 1 leak detection system EFR notified the DRC verbally on June 3, 2010 by telephone and m writing on June 7, 2010 by letter, fulfilling the notification requirements of Part IG 3 of the GWDP The volume of fluid detected constituted a violation of Condition 11 3 of the 195 North 1950 West • Salt Uke City, UT Mailing Address P O Box 144850 • Salt Lalce City, UT 84114-4850 Telephone (801) 536-4250 • Fax (801) 533^097 "TDD (801) 536^14 www deq Utah gov Pnnted on 100% recycled paper Page 2 RML, tnggenng the requirement to notify the DRC, to identify the cause of the violation, and to implement remedial action EFR lowered the solution level in Cell 1 to facilitate inspection and of the flexible membrane liner (FML) Dunng June and July, 2010, EFR completed repairs of defects it identified in the FML Believing the repair to have succeeded, EFR raised the solution level in the cell, only to detect fluid in the LDS again on August 7, 2010 Dunng a conference call on August 12, 2010, EFR and the DRC agreed that the repair effort had not identified and corrected all defects in the FML, necessitating further corrective action EFR assembled a repair plan which it submitted to the DRC on August 18, 2010 DRC review and subsequent negotiation led to EFR submitting a revised repair plan on August 30,2010 The DRC approved the plan, with modifications, through a Confirmatory Action Letter on September 22,2010 (the CAL) EFR lowered the solution level to elevation 5613 feet above mean sea level (AMSL), and completed repairs in stages dunng the summer months of 2011 and 2012 Findings and Recommendations The Mill's Liner Mamtenance Provisions, Revision 1, dated October 18, 2009 (LMP), contain a number of requirements for liner repair, including 1 EFR must submit a repair report The CAL required EFR to include this report with the 2"^* Quarter, 2012 DMT Performance Standards Momtonng Report The DRC received the DMT Report, including the repau" report, on August 27,2012 This action both fulfills the requirement to report and the deadline by which to report repair activities to the DRC 2 The LMP requu-es a repau* report to bear the seal and signature of a professional engineer registered in the State of Utah Harold Roberts signed and sealed the report 3 The LMP requires the report to include a descnption of the damage discovered and the work completed to repair that damage The report attempts to fulfill this requirement Because the imtial, limited repair effort proved ineffective, the repair plan evolved to replacement of damaged sections of liner above elevation 5613 AMSL Thus, the descnption of specific damage and local repairs pertained only to the imtial, failed attempt The liner failure appeared to result from wear and tear imposed by foot traffic (sampling, momtonng, etc ), movement of discharge hoses and solution transfer over the 30-year life of the liner The nanative and attached documentation highlights typical damage encountered, and includes photographs of typical examples, rather than documentmg in the report all defects identified Documentation of all defects exists at the mill's offices I am satisfied with the narrative, given the extent of the repair effort 4 The report must include specifications for matenals employed in the repair The onginal FML consisted of 30 mil PVC roll stock EFR chose a 320 mil PVC roll stock from Colorado Lming, Inc for the replacement matenal Following removal of damaged sections of liner and preparation of subgrade to receive the Imer, the repair crew cleaned the existing matenal at the site of the seam with methyl ethyl ketone Crews then cut a patch from the roll stock and cemented it to the existing liner matenal using an adhesive supplied with the roll stock The matenals appear appropnate for the repair effort "\ 5 Repau- patch seams must perform satisfactonly under the vacuum test method ASTM D5641 The report includes a tabular presentation of all seam tests, and a narrative interpretation of the results Page 3 All seams received testing, with test sites overlapping so as to eliminate the possibility of omitting any seam length from evaluation No vacuum leaks appear in the test logs 6 Daily reports of repair work must appear m the repair report Appendix 4 to the repair report includes typewntten transcnptions of the daily reports 7 Quality assurance/quality control assessments must receive treatment in the report narrative As I understand the terms, quality assurance refers to methods employed in the work to assure production of a result meeting specified standards of quality Quality control mvolves observational methods, inspection and testing among them, to detect deviation from quality expectations and offer opportumty for corrective action Quality assurance should be ongoing, while quality control can be episodic Dunng a field mspection on September 20, 2012,1 quened David Turk and Gamn Palmer about the repair effort Both, mdependently, cited the challenges of traming crews to perform the work correctly, and the need for continuous rather than episodic inspection in this case For example, all lengths of all repau* seams received vacuum box testing per ASTM D5641 as soon as the adhesive had set, and any defects received immediate attention, the entire patch was removed and replaced upon discovery of a leak, no matter how small, rather than nsk further failure of the seam I am satisfied with the quality assurance and quality control activities EFR employed 8 The repair report must appear in the quarterly DMT Performance Standards Momtonng Report for the quarter following that in which the repairs conclude Repairs concluded on June 4, 2012, the last month of the 2"'* Quarter In the CAL, the DRC required completion of repairs on or before July 31, 2012 The repairs concluded eight weeks ahead of deadline, and the repair report appears one quarter ahead of deadlme In addition to the above requirements, the CAL stipulated inclusion of a root cause analysis m the liner repair report A root cause analysis appears as Part 3 to the report, identifying defects and damage The root cause analysis further clanfies the damage as the likely result of foot traffic fi-om sampling, momtonng and other such activities, effects of discharge hoses and solution transfers, and exposure to weathenng conditions not expenenced below the operating fluid level of the cell The explanations presented seem reasonable Finding Given the above analysis, I find both the report and the repair effort it chronicles to meet expectations, as nearly as can be ascertained at this date Only actual testing under field conditions will ultimately prove the effectiveness of the repau* effort Recommendation I recommend approval of the repau* report, and the underlying repairs I recommend retaimng the file open until the solution level in Cell 1 reaches maximum design working elevation and results of routine momtonng of the leak detection system support a conclusion that the repairs have succeeded Thirty days from the date the fluid level reaches design maximum elevation should suffice