HomeMy WebLinkAboutDRC-2012-002550 - 0901a06880339544DRC-2G12-002550
ENERGYFUELS
Energy Fuels Resources (USA) Inc
225 Union Blvd Suite 600
Lakewood, CO, US. 80228
303 974 2140
www energyfuels com
VIA EMAIL AND OVERNIGHT DELIVERY
December 21, 2012
Mr Rusty Lundberg
Director of the Utah Division of Radiation Control
State of Utah Department of Environmental Quality
195 North 1950 West
P O. Box 144850
Salt Lake City, UT 84116-4850
Re: White Mesa Uranium Mill - Notice of Violation and Corrective Action Order
UDEQ Docket No. UGW-20-01
Notice Pursuant to the Chloroform Pumping Well Operations and Maintenance Plan
Dear Mr Lundberg
Pursuant to the White Mesa Mill's (the "Mill's") Chloroform Pumping System Operations and
Maintenance Plan ("Chloroform O&M Plan") Energy Fuels Resources (USA) Inc , ("EFRI") as operator
of the Mill, is providing written Notice to the Utah Division of Radiation Control ("DRC") of a
temporary outage in two chloroform capture pumps, as descnbed in more detail below
The Mill's Chloroform Pumping O&M Plan states that EFRI will notify DRC of system failures that
cannot be made operational withm 24 hours of discovery It was determined on Wednesday, December
19, 2012 that a transformer failure had occurred which would require more than 24 hours to be repaired
The failure shut down electrical power to two chloroform continuous pumping wells which will be off
(not pumping) until the transformer is replaced or an interim source of power is provided Imtial notice
of this outage was given by telephone to Mr Dean Henderson of DRC at approximately 3 40 pm on
Wednesday December 19,2012 (v^thm 24 hours of the discovery).
1. Description of the Pumping System Failure
a) The Mill's Chloroform O&M Plan, submitted on October 25, 2010 and currently under review
by UDEQ, states that Denison will notify UDEQ of system failures that cannot be "repaired
and fully made operational within 24 hours of discovery "
b) The Mill expenenced freezing temperatures for most of the week of December 17, 2012
Temperatures reached single digits on December 19, 2012
Letter to Rusty Lundberg
December 21,2012
Page 2 of4
c) One of the power circuits to the Cell 1 area supplies power to MW-26 and TW4-20 This
circuit includes a transformer near the Mill's truck shop
d) Mill personnel discovered, at approximately 10*30 am on December 19, 2012, that the truck
shop transformer had failed when power to several areas of the Mill, including the tailings
area, failed.
e) MW-26 and TW4-20 pumps stopped when power was lost There was no apparent damage to
the pumps or flow measurement instrumentation; however pumping will cease until power can
be restored to the affected circuit
f) Dunng the mormng of December 20, 2012, Mill management determined that a replacement
for the damaged transformer would require up to 2 weeks or longer for delivery to the Mill
site
g) On December 20, 2012, Mill management began moving gasoline dnven generators to supply
the Cell 1 area and reactivate the well pumps until the replacement transformer amves and is
installed Installation ofthe generators was completed dunng the night shift on December 20,
2012. The well heat lamps were tumed on to thaw any frozen well water
h) Immediately following confirmation that no frozen areas remained in the pumping system, the
well pumps were tumed back on at approximately 3 00 pm on December 21,2012
2. Root Cause
The root cause analysis is as follows
a) A failed transformer caused a loss of power to the circuit which includes MW-26 and TW4-
20
b) The replacement transformer could not be acquired and installed within 24 hours ofthe initial
power loss
c) The installation of the temporary generator and thawing of the well piping prior to
resumption of pumping required longer than 24 hours
3. Period of Time the System Was Not in Operation
At the time of wnting of this Notice, the pumps ceased operation for approximately 54 hours from
December 19 to 21, 2012
Letter to Rusty Lundberg
December 21, 2012
Page 3 of 4
4. Date By Which the Pumping System Will Be Repaired and Operational
Pumping was resumed on December 21, 2012
5. Steps taken to Repair and Have the System Fully Operational
a) Mill maintenance personnel isolated the failed electncal circuits on December 19, 2012
b) Mill maintenance personnel located on site several portable gasoline-dnven electnc
generators throughout the day on December 20, 2012
c) Two generators were placed at the Cell 1 area on December 20, 2012 One generator was
vsdred to supply both of the affected pumping well pump motors
d) Maintenance personnel set up the heat lamps to thaw any potential frozen piping around the
two affected well pumps
e) The two affected well pumps were tumed on and resumed pumping at approximately 3 00
pm on the mormng of December 21,2012
f) The portable generator supplying the two affected well pumps will be left in place until the
replacement transformer amves, is installed, and power is restored to the Cell 1 area
electncal circuit
6. Additional Factors to Be Taken into Account
Although this incident does not fall within UAC R317-6-6 16, EFRI believes that the following should
be taken into account by DRC in evaluating this incident
a) Notification
By virtue of the initial oral notification given to DRC at 3 40pm on Wednesday December 19, 2012
(within 24 hours of the discovery) and this written notice, EFRI has submitted notification according
within five days
b) Failure was not Intentional or Caused by EFRI's Negligence
The failure of the pumping system was not due to negligence on the part of EFRI or Mill personnel
The failure resulted from an unavoidable condition, specifically, failure of a transformer occumng
dunng continued freezing weather
c) EFRI has Taken Adequate Measures to Meet the Conditions of the Chloroform O&M Plan
EFRI has taken adequate measures to meet Permit conditions in a timely manner Mill personnel
notified Corporate Compliance personnel within hours of the incident. DRC was notified on the same
Letter to Rusty Lundberg
December 21, 2012
Page 4 of 4
day as the incident, and within 24 hours. Mill personnel immediately located and ordered a
replacement transformer. Mill personnel located and moved temporary generators to the Cell 1 and
well pump area within hours of determining that delivery time for the replacement transformer
Hookup ofthe generator for the two affected pumps, thawing ofthe line, and restart ofthe well pumps
was performed within less than three days from the initial power loss.
d) The Provisions of UCA 19-5-107 Have Not Been Violated
The provisions of Utah Code 19-5-107 have not been violated There has been no discharge of a
pollutant mto waters ofthe state EFRI has not caused pollution which constitutes a menace to public
health and welfare, or is harmful to wildlife, fish or aquatic life, or impairs domestic, agncultural,
industnal, recreational, or other beneficial uses of water, nor has EFRI placed or caused to be placed
any waste in a location where there is probable cause to believe it will cause pollution
If you have any questions, please contact me at (303) 389-4132
Yours very tmly.
ENERGY FUELS RESOURCES (USA) INC.
Jo Ann Tischler
Manager, Compliance and Licensing
cc David C. Frydenlund
Phil Goble
Dean Henderson, DRC
Dan Hillsten
Harold R Roberts
David E Turk
Kathy Weinel
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